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Freeport LNG gas consumption running near no for 5th day

Freeport LNG's. liquefaction plant remains primarily offline for a fifth straight. day, with gas usage rates at 125 million cubic feet per. day (mmcf/d), or 5% of its completely functional usage, data from. monetary company LSEG showed on Monday.

Freeport LNG has actually been the second-largest U.S. LNG exporter,. with an installed capacity of 15 million lots per annum (MTPA),. however mechanical problems and repair work to its Quintana, Texas,. plant added to minimized U.S. LNG output in February and. March, the data reveal.

Freeport LNG did not right away reply to an ask for. remark.

Because completion of January, Freeport LNG has actually run at. significantly lowered capability, with only two of its three. plants, called trains, working, and in March that was up to one,. the data showed.

Natural gas utilization in February and part of March for. Freeport was up to about 1.3 billion cubic feet each day (bcf/d). and then to 700 mmcf/d, suggesting only one train was working,. the data showed.

The plant draws between 2.2 bcf/d and 2.4 bcf/d when totally. operational. Gas costs at the Henry Center exchange were trading. down 5 cents at $1.718 per million British thermal units on. Monday.

On March 20, Freeport said its Train 2 liquefaction system had. been shut down, while Train 1 will be taken down imminently as. it anticipates inspections and any subsequent repair work at both the. systems to be finished by May.

The systems were to be taken offline on the go back to. production of its Train 3, that was secured of service when. its motors were damaged during a January freeze, Freeport had. stated.